I upgraded from Marlin 1.9.x to 2.0.7.
- I am using an Einsy Rambo with integrated TMC2130 drivers. I literally used the same currents from the 1.9.x version on the 2.0.7 and the motors barely have strenght to move.
- How is this possible? Is the new marlin managing current in a different way?
I am using stealthchop on both versions.
XYZ Current 700
E0 Current 800
Those values are the same on both 1.9.x versions and 2.0.7.
Cheers,
JJ